Tuesday, July 9, 2013

front door window replacement on a Mazda mpv




The front right window of our 2003 MPV shattered. I decided to replace it with used glass for $35 instead of the $190 price that the local window shops where charging. Car-part.com is a good place to look for salvaged parts. Just be sure to filter for parts closest to you.
I never did figure out exactly why the window broke.
Pry off this plastic piece with a small screw driver. Note the two bolts holding on the mirror.

Remove the screw from the handle.

Remove the door light cover and one screw inside.
If you leave the door open  long enough then the  light will turn off and not burn you .

Remove the screw from the arm rest. Mine was hiding under this matt. 
I will add pictures of the 2 or 3 plastic screws along the back of the door. After they are out you can start gently removing the door cover. There are several plastic grommets. Turn the door latch side ways and push it through it's hole.
Remove the plug for the window controls, and the wire for the door light. It is hot if it has been on. I removed the bulb after it melted a hole in the weather barrier plastic.

Here is a closeup of the window switch. I had to remove it from the door panel so I could roll the window down.
Fold back the plastic weather barrier and roll the window down until you can access both screws for the glass.

Here is the plastic piece that goes through the glass. My new glass came with some already attached, but I would save them until you get your new glass.

I did not take any pictures of the installation of the glass. There are some YouTube videos showing how to install window glass. Basically you angle the front of the glass down about 45 degrees, and put it slowly down inside the door until the back of the glass can fit inside the track. Then rotate it back into position. Be ready to grab the glass from the bottom and guide it into place. I did this by myself, but a second person could be useful. While you have the door panel off it would be a good time to apply some white lithium grease to the window regulator cable and other moving parts.

Wednesday, September 28, 2011

How to replace a vacuum breaker on a toilet

If you are like me you have used industrial/commercial type toilets hundreds or thousands of times without giving a second thought about how they work. I have now had some experience working on them, and while  I am still no expert, I do have the knowledge to work on them.

Vacuum breakers in industrial/commercial type flush valves are what seem to wear out the most in my experience. Some signs of a warn out vacuum breaker are:
  • Water leaking from the top of the pipe where it joins the bottom of the flush valve
  • Flushes taking too long or not stopping.
  • Having to hold the handle down for the flush to complete.
  • Unusually loud flushes.

The first thing to do is to shut off water. remove the cap.


Use a flat head screw driver to turn the water off. Turn clockwise.
Loosen the union. Use an adjustable wrench instead of this kind.

Or you can use a clothe to keep from scratching the fixture.
Unscrew the lower union. and remove the flush assembly.

Here are the three pieces of the new vacuum breaker.

Vacuum breaker shown installed. Makre sure to clean the pipe before putting the vacuum breaker in place.
Replace the flush valve and tighten the unions, making sure they are nice and tight. If they are not tight or the pipe is dirty that could cause the pipe to leak, or the toilet to keep flushing. After the joints are tight turn the water back on and check for leaks. I put some teflon tape on this one, because it would not stop leaking without it.

Technotrans beta.c

I was called into look at the Technotrans beta.c unit that cools water for our Manroland sheet fed press. I was told that the water temps were too high and that they had reset the high pressure switch on the compressor, but were not sure if it had helped. I went outside to make sure that the condenser fan was working like it should, which it was. The compressor was cycling on and off over, maybe a 30-40 min period (not short cycling). I put the refrigeration gauges on and checked the pressure. The pressure was well below the limit of the high pressure cutoff switch.

Time to call the tech.
I call Technotrans and explain the problem. The tech wants the serial number so as I am looking for it, opening doors, I see another compressor. He says, yes the smaller compressor on the left is the one that cools the chill water. I pushed the red reset button, and what do you know, it comes on and starts cooling the water. The tech tells me that I should check the pressure  on this one as well. If the pressure is in the 250-270 range then there is an oriface that needs to be cleaned. I measured the pressure and it was in the 200 psi range which is good.
This is the compressor that was tripped, and the on that controls the chill water

To the left of the brass 90 degree elbow is the orafice that would have needed cleaning.
So, call that tech, it is what they are there for. I wanted to get all the information about the problem before calling, but I was getting information about the wrong compressor.

Wednesday, September 14, 2011

new blog

I have started a new blog at mynewfixation.blogspot.com . This will be a place where I post about my latest fixation, usually tech related.

Thursday, September 8, 2011

Calibrating a pneumatic thermostat

Pneumatic thermostat

Tools needed: thermometer, Allen wrench tool, and needle pressure 
gauge
Use the Allen wrench tool to remove the cover. Turn clockwise to  turn the screw into the  base allowing the cover to slip over the head of the screw.
Adjust the temperature so that the edge of the black dial is lined up with the measured temperature. This one is set  just below 76 degrees.
Push pressure gauge into the hole as shown. Insert Allen tool into adjustment screw. Adjust until the gauge reads 9 psi. Be careful, adjust slowly, it is also sensitive to the heat from your hand.

You can also adjust the temperature reading on the front display, so that it will better reflect                                                   the actual temperature of the room.






Friday, September 2, 2011

Repair Becker vacuum pump

Repair a Becker DVT 3.140 vacuum pump bearing.

Vaccum pump number 4 was tripping the breaker. The pump was hot to the touch and when it was turned back on there was a loud noise comming from it. My first thought was that it had broken vanes.
I found vanes online, while waiting for it to cool off.The the part number is 90133400 and the DVT3.140 requires 7 and the dimensions are 240 x 43 x 4.0 I found them at this site http://cfpwarehouse.com/shopsite_sc/store/html/vane_chart_becker.html

We took the cover off. And the vanes were fine.
We did find a piece of epoxy inside the fan. It looked like was used to keep the fin tubes in place.

We took the other end off to check the bearing. It was not getting any grease and was really bad.
The grease line from the zerk to the bearing went the whole length of the pump so we shortened it. Hoping that the grease wouldn’t have a chance to heat up and cook inside the line.
vane end of pump, with cover and bearings removed.

Broken epoxy that was stuck in the fan.
Pump with all covers removed. The grease zerk on the other end of the pump had a grease tube connecting it to the bearing on the close end of the pump.

New location, and shorter grease tube.

Motor side of pump with bearing covers and motor mount removed.
We replaced both bearings on each end. skf 3206a/c3 and nu 206ecp/c3

Thursday, September 1, 2011

First Post

I am not really sure where I should start. I am thinking that this blog will start off as a place for me to keep track of work projects. I work as a maintenance technician on a lot of different machines and equipment. In the past I would figure out what was wrong with a piece of equipment and get it all fixed up. Then 6 months or a year go by and the same problem comes up again, and although it seems familiar I would not remember what I did to fix it the last time. So I started keeping a written record of what problems I was encountering and what it took to fix them, phone numbers of service techs, web sites with information about the product, manuals and schematics. I also started taking pictures of the machines, especially if they were difficult to take apart or put back together. Will this be of any value to anybody besides me? I hope to find out.

I have a few other ideas for this blog. I like taking apart and fixing stuff, thus the title of the blog "The Tinkerist". As I find broken stuff to fix I will take pictures of the process and explain how I fixed it. The computer that I am typing this on is completely salvaged from the scrap heap except for the wifi adapter.